Quick and easy ELT search..

July 3, 2007 on 9:23 pm | In General | 5125 Comments

I had to drive to the hangar to pick up my radio gear to home this one, but driving into the airport I could see a plane being worked on in the Avionics shop.  I had a hunch that it would be in there..

Once I had my radio, I drove straight to the Avionics Shop, and walked straight up to the plane with the ELT signal..

The total time from getting the phone call at home, to having the ELT turned off must have been under 15 minutes..  Now that’s got to be a record!  

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June 18 19:21
Task# 700225

SWE AIR ELT 2 2 PEP Air members responded to locate an ELT that was sounding in the Pitt Meadows Airport area.  Transmitter was located in an aircraft where it was recently installed and turned on. Members silenced the signal.

Homing a Greyhound bus?

July 3, 2007 on 9:20 pm | In General | 104 Comments

 A challenging one..

I was dispatched by JRCC to locate and ELT that was sounding in the Langley area, however Langley Tower couldn’t hear it.  I took off from Pitt Meadows, and flew over mid-field at Langley at 2000′.  I could hear the ELT, but it was just not strong enough to be located on the field, and tower was still reporting that they heard nothing..   After a few minutes of working the signal, I determined that it was located about 2 miles West of Langley airport, which puts it right in the middle of downtown Langley..  A quick search of the database in the GPS showed that my location was 0.2km from the Langley Greyhound depot.   I landed at Langley and took a taxi to the depot, but the signal was gone…  The staff at the depot informed me that a bus had just left recently with packages destined for the sorting depot in Coquitlam.   So I went back to the airport, and took off towards Coquitlam.  As I was over Surrey I was starting to pick up the signal again, and sure enough, it was strongest right over the Coquitlam Depot..   I turned the plane for Pitt Meadows, landed and put the plane away, then jumped in the truck and drove to Coquitlam..  Upon arriving at the depot in Coquitlam the signal was quite strong, it took about 10 minutes to narrow it down to a specific package..   And sure enough, the package was being shipped from a Helicopter outfit in Langley to have the ELT re-certified..   The ELT wasn’t packaged properly, and was probably activated before it even left the hangar.

The official report below was very short and sweet..   As with all of these events, there’s much more to the full story..

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June 12 15:56
Task# 700209

SWE AIR ELT 2 2 Southwest PEP Air members responded to locate an ELT sounding at the Langley Airport. Members went airborne and ELT was homed to a bus depot in Coquitlam. The package was opened and the ELT was turned off.

Airborne ELT search

May 20, 2007 on 4:14 pm | In PEP Incident Reports | 5410 Comments

This was my first tasking as pilot on an ACTUAL search.  Less than 1 hour from wheels up, to ELT located, to wheels down.

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May 13 14:46
Task #700117

3 PEP Air members responded to locate an ELT sounding in Langley. The ELT was homed in to a US aircraft in flight. The signal was silenced once the aircraft was on the ground at Blaine Airport.

ELT ground search at Pitt Meadows

May 6, 2007 on 3:58 pm | In PEP Incident Reports | 6651 Comments

April 13  18:36
Task #700035

1 PEP Air member responded to locate an ELT sounding near the Pitt Meadows Airport. The ELT was located and turned off.

 

 

FEFY flies again!

April 14, 2007 on 8:59 pm | In Aviation | 21752 Comments

Thursday afternoon I made the first flight with the engine re-installed.  The performance was unbelievable, it was like flying a completely different airplane.

It’s Saturday evening now and I have just over 5 hours of flight time on the engine.

My previous full throttle speed was 100kts, I’m now getting 120kts.  Quite a significant increase.

Here’s a few assorted photos of the engine installation and interior cleanup.

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img_4548-large.JPG  fefy-rebuild-037-large.jpg  fefy-rebuild-033-large.jpg

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The Engine arrives!!

March 30, 2007 on 7:39 pm | In Aviation | 5024 Comments

I picked up the engine today..   Here’s some before.. And after photos.

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Ken has certainly performed his usual magic in rebuilding the engine.  The performance promises to be comparable to the appearance of the engine based on the 1 hour test run that was done at the shop.

Engine ready for pickup..

March 27, 2007 on 9:48 pm | In Aviation | 5104 Comments

I got the call from Ken Vike at Vike Aeromotive yesterday.  The engine had just been fired up and run on the test cell at the engine shop. 

Ken reported that the engine was running great, and was in fact turning the test prop 30-50 RPM faster than average.  That translates into extra horsepower when the engine is able to turn the prop faster. 

I’m really excited to see the difference in performance in the plane once it’s all back together.  The engine was originally 150hp, with all the upgrades and the tuned exhaust I’m expecting to be producing about 180hp. 

The engine has been stripped of all the old paint and repainted with colours to match the stripes on the plane.  Photo will be posted soon!

 

Engine upgrade continues..

March 27, 2007 on 9:40 pm | In Aviation | 255 Comments

The plan of a simple installation of a new exhaust has grown into a major production.

The original plan was to order the PowerFlow exhaust, and while waiting the 3 weeks for it to arrive install high compression pistons. 

In the process some corrosion was spotted on the cam followers inside the engine, which then meant it was time for the dreaded “bottom overhaul” on the engine..  Then since the engine was off, I might as well strip the engine mount, have it NDT’d, and repainted.  I also sent the oil cooler out for overhaul, and the alternator.  Most parts on the plane have only been in service for 1000 hours, which isn’t much, but considering that it was over a 30 year period, they were due to be checked over..

While waiting for all the parts to come back from their overhauls I stripped the paint off the firewall, and repainted the lower half, and polished the upper half.  It took a lot of effort, but I think the result was more than worth it!

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 I also didn’t like the look of the forward float fittings, so I removed them.  Very good thing I did as there was a lot of hidden corrosion.  Fortunately it was caught in time, another year and it would have become very expensive to repair the aluminium skins.

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On the inside of the plane, the lower left engine mount bracket and stringer were showing signs of corrosion.  About 60 rivets had to be drilled out to remove the parts.  Again fortunately the corrosion was caught in time and the parts were able to be restored.  If you look at the first photo below, you can see the rust on the steel fitting.  The aluminum in contact with the steel was also starting to corrode.  The 2 parts would have cost about $700US to replace with new ones.  How’s that for incentive to keep on top of any corrosion you might spot!

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 When Cessna built the plane in 1973, fiberglass insulation was glued to the inside of most of the cabin.  It’s common practice to remove all the original insulation these days and replace it with a fireproof type of closed cell foam.  The fiberglass tends to hold onto any moisture, and keeps it in contact with the aluminum.  A perfect example of this was the bottom side of my glareshield.  I was replacing the hoses in the vacuum system when I decided to remove the fiberglass insulation in this area, here’s what I found:

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The brown colour is the remains of the contact cement and fiberglass insulation, the corrosion is the white powdery looking stuff.  A couple hours of cleanup and re-paint and this area will be like new again.

While I’m showing the worst of the problem areas in my photos, the plane is in great shape.  I’m really happy to be finding and correcting all these issues before they become more serious.

More engine pics…

February 4, 2007 on 4:52 pm | In Aviation | 5507 Comments

img_4209-medium.JPG img_4211-medium.JPG img_4207-medium.JPG img_4208-medium.JPG

img_4216-medium.JPG Painting some parts..

img_4214-medium.JPG img_4215-medium.JPG Installing the ADC oil filter.

FEFY gets more Horsepower!

February 2, 2007 on 10:36 pm | In Aviation | 774 Comments

Rachael and I did a day trip to Oliver, BC last weekend.  Enroute I noticed that the CO detector was showing signs of exhaust gas in the cockpit.  Shutting off the cabin heat resolved the problem for the remainder of the flight.  That night I pulled the exhaust off the aircraft and found two small cracks where the exit stack meets the muffler can.  

I’ve had two upgrades for the engine in mind since buying the plane.  First I wanted to install high compression pistons, which take the engine from 150hp up to 160hp.   Later I was planning to add a PowerFlow tuned exhaust system, which claims to add a further 23hp.   With the crack in the exhaust it changed my plans around and it appeared that the exhaust was now going to come first..  After thinking it over for a couple days I came to the conclusion that I might as well just do both upgrades in one shot..  The timing is good being winter and only flying the plane a couple times a month recently, better now than in the middle of summer.  The timing works well to install the ADC oil filter system, all my parts have arrived to start that install.

So…  Here’s how the plane looks 6 days later..

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 img_3644-medium.JPG Just for reference..  Here’s how the engine looks when it’s all together.

I’ll post more pictures as parts arrive and things start going back together.

 

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